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BA B777 short of runway @ LHR

FrankTheTank

Professional Pot Stirrer
pilot
New Information

Internal inspections of the fuel tanks were done. The only anomalies were a loose B-nut on a sensor line for the fuel scavenge system and a plastic scrapper near a suction feed port.
These findings are not significant. Fuel sample analysis continues to show the fuel is within specification. The investigation continues to look broadly for a cause of the dual engine rollbacks. Fuel exhaustion is the only item that has been positively ruled out. Aspects that the FAA believes the investigation is concentrating on are:

Ice in the fuel somehow limiting the fuel flow to the engines. A maintenance message indicating excessive water in the center tank was set during taxi on the two previous flight legs, although it cleared itself both times. The airplane was being operated in a high humidity, cold environment, conducive to ice formation.

Small-sized contamination building up in the engine fuel systems somehow limited the fuel flow to engine. All the fuel samples have tested for contamination of larger particles (sizes outside the fuel specification). Testing has been started looking for small particles (greater than 5 microns).

Engine hardware failures sending inaccurate data to the engine electronic control (EEC) causing the EEC to demand insufficient fuel. A preliminary review of the EEC data from the right engine shows erratic combustor inlet pressure (P30). A leaking P30 sense line could cause this, or the EEC receiving a higher than actual fuel flow
parameter.

Software coding problem in the EEC causing the EEC to demand insufficient fuel.
British Airways installed a new engine EEC software revision in December 2007. The software was approved in May 2006. There were several changes to the software as part of the revision. Two items seem remotely related to the accident: improvements to low power stall recovery logic and fan keep out zones for ground maintenance
 
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